

Ship 40's common dome section has arrived at Mega Bay 2. pic.twitter.com/fCHArlA3OQ
— Avid Space (@LabPadre) February 12, 2026
Another section of Super Heavy Booster 20 has been brought out of Starfactory and taken into Mega Bay 1. pic.twitter.com/p9U43CSEwo
— Avid Space (@LabPadre) February 12, 2026
We just released a comprehensive video report explaining the status of @SpaceX's two Gigabays, purpose-built for the mass production of Starship.
— RGV Aerial Photography (@RGVaerialphotos) February 11, 2026
Written by @BJSchnettler! Watch it here:https://t.co/6a4hCK93M3 pic.twitter.com/673NoWo6aI
Correction: Four times.
— Casey Handmer (@CJHandmer) February 13, 2026
double aught said:
Why would there have been total loss on a human flight? This one kept going.
Rapier108 said:double aught said:
Why would there have been total loss on a human flight? This one kept going.
On the shuttle, we saw what happened with a SRB burn through with Challenger.
Since SLS does have a launch escape system, they might be able to get the capsule clear before failure, or before the RSO blows it up.
Holy crap... I don't think any rocket should be overflying that much populated area until it's flown a few hundred times without a RUD on ascent. I would not trust Starship for a while. All it takes is one Flight 6 or 7 incident to have heavy debris falling over populated areas.
— Everyday Astronaut (@Erdayastronaut) February 13, 2026
Quote:
The 2024 booster malfunction occurred on the Vulcan rocket's second test flight. The rocket did not return to action for 10 months as engineers probed the nozzle failure. Investigators determined that a carbon composite insulator, or heat shield, inside the nozzle failed to protect the nozzle's metallic structure from the superheated exhaust coming from the booster. Engineers traced the cause of the failure to a "manufacturing defect" in one of the insulators, which led to the melting and burn-through of the booster nozzle. Officials said the damaged motor continued firing on the 2024 launch, albeit with less thrust and lower efficiency, and the Vulcan's BE-4 main engines, supplied by Blue Origin, compensated for the thrust differential. The BE-4s on Thursday's flight appeared to save the rocket once again.
ULA officials last year said they inspected other boosters in the company's inventory to ensure they did not exhibit the same defect. The incident on Thursday's mission suggests the defect was not fixed, or there is a separate problem with Northrop's boosters.
Rapier108 said:double aught said:
Why would there have been total loss on a human flight? This one kept going.
On the shuttle, we saw what happened with a SRB burn through with Challenger.
Since SLS does have a launch escape system, they might be able to get the capsule clear before failure, or before the RSO blows it up.
Ag_of_08 said:
They would, most likely, have tripped the LES and attempted an abort i would think. I really don't know what the abort windows look like on that vehicle though.
txags92 said:Rapier108 said:double aught said:
Why would there have been total loss on a human flight? This one kept going.
On the shuttle, we saw what happened with a SRB burn through with Challenger.
Since SLS does have a launch escape system, they might be able to get the capsule clear before failure, or before the RSO blows it up.
SRB burn through at a mid body O-ring is not the same as an engine nozzle burn through. Both are certainly dangerous, but not to the same degree.
Ag83 said:txags92 said:Rapier108 said:double aught said:
Why would there have been total loss on a human flight? This one kept going.
On the shuttle, we saw what happened with a SRB burn through with Challenger.
Since SLS does have a launch escape system, they might be able to get the capsule clear before failure, or before the RSO blows it up.
SRB burn through at a mid body O-ring is not the same as an engine nozzle burn through. Both are certainly dangerous, but not to the same degree.
According to who?
Just to be clear here, NASA declared its recent test a "successful wet dress rehearsal" despite missing its T-30s target by almost five minutes, botching the dreaded Orion hatch close out procedure, and managing to achieve up to 16% H2 due to copious leakage at the fueling… https://t.co/ROk9OJ84Nb
— Casey Handmer (@CJHandmer) February 14, 2026
Ag_of_08 said:
The segmented SRBs survived several seal failures/extremely close to failures. Boisjoly and others at Thiokol had been warning about them for quite a while.
The fact a failure didn't destroy a vehicle is not proof of the severity of the malfunction.